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21/11/2011

Thursday 17th November 2011 - Sunday 20th November 2011 : Omniblog

Yes another omnibus edition , thanks largely to the X1 fleet behaving themselves. I was out sampling beer with Peter last night and he said "When you do several days in one entry in the blog, can you do the days in reverse, otherwise it seems in the wrong order". Well I've had a long think about this and the answer is No ! Oh Dear that's another friend I've lost - and my oldest one at that. I don't think I could handle writing it backwards Peter it's as simple as that. Anyway, see what you think of this :

Thursday 17th November

Punctuality was quite good, with 3-4 minutes being the average delay. 37157 on L11 passed me 10 late at 11.30, but by the time it returned from Peterborough (due by me at 12.50) it was just a minute late.
37579 was 12 late into Lowestoft with Y7 and departed 4 late on the return 14.55 to King's Lynn says Malcolm. 37574 on Y6 was changed for 37575 at some point while 37160 was off the road at Lynn for repairs.

Friday 18th November

37574 was at Vancouver Avenue today for its turbocharger to be replaced. 37160 was back in traffic on K3. There were some unusual diversions around Wisbech this afternoon. K15 with 37568 was spotted by me coming in from Peterborough about 14 late at 15.04 through the Old Market having travelled via Wisbech St. Mary and then Jamie R saw K2 coming in to the town over the Norwich Road speedbumps with 37566 at around 16.20.
Until L12 services through Wisbech seemed to run well, but Y13 with 37570 was viewed on Lynn Road running 13 late on the 13.56 to Lowestoft. K14 ws also delayed and was 19 late in from Peterborough for the 14.26 eastbound.
As usual on a Friday, K16 saw the heaviest delay and fittingly it was dear old 37159 in charge of the 14.35 ex Peterborough, seen arriving Wisbech 31 late and then viewed 28 late at Walpole by Bruce. & Rob Brooks.
K17 and 37576 ran 21 late eastbound but after this services gradually returned to normal.

Saturday 19th November

An incident on the A47 between Wisbech and Guyhirn saw the road closed until 15.30 today. All services were diverted via Wisbech St. Mary. 37160 was kept at Lynn garage with its interior lights malfunctioning and 37563 also had a day off here for attention to some panels.
'First' seem to have decided that it's about time they challenged Konectbus on fair promotions , both Des and Sam sent me this link :
http://www.firstgroup.com/ukbus/suffolk_norfolk/travel_news/news_initiatives/?item=3511

Sunday 20th November

An all B9 operated service with minimal delays noted. 37565/7/8, 37571/2/3/4/5/8/9 were the buses used. 37572 is now the highest mileage B9, it has now done just over 368,000 miles !

1 comment:

jim long said...

Hi Gerard..

i noticed you mentioned that 37574 had to have a replacement turbo,is this often happening?? if so,it may be that when they first start up they rev the engine in order to get the air up,where as they should let the bus idle for at least 2-3 minutes in order for the oil to get to the bearings on the turbo,it's so easy to overlook the poor ole turbo and go straight into rev mode..